-6.2 C
New York
Sunday, December 22, 2024

Is the Well Integrity Test Failing?

Is the Well Integrity Test Failing?

Courtesy of Washington’s Blog

BP suspended the "top kill" operation for 16 hours – because, according to numerous experts, it was creating more damage to the well bore – without even telling the media, local officials or the public that it had delayed the effort until long afterwards.

BP also admitted – many days after it stopped the top kill attempt – (1) that BP had to stop because mud was leaking out below the seafloor, and (2) that capping the well from the top could blow out the whole well.

Similarly, it took more than 5 hours for BP to publicly announce the delay of the "well integrity test" after the decision to delay was made.

So BP doesn’t have a great track record of promptly informing us of what is happening.

But now that the well integrity test (background here and here) is underway, can we somehow tell if it’s working or not?

The government previously announced that the test would succeed if pressure in the well of 8,000-9,000 psi were observed for a sustained period. As Coast Guard admiral Thad Allen said:

We are looking for somewhere between 8,000 and 9,000 PSI inside the capping stack, which would indicate to us that the hydrocarbons are being forced up and the wellbores are being able to withstand that pressure. And that is good news.

If we are down around in the 4,000 to 5,000, 6,000 range that could potentially tell us that the hydrocarbons are being diverted someplace else, and we would have to try and assess the implications of that. And as you might imagine, there are gradations as you go up from 4,000 or 5,000 PSI up to 8,000 or 9,000. …

We will at some point try to get to 8,000 or 9,000 and sustain that for some period of time, and these will be done basically, as I said — if we have a very low pressure reading, we will try and need (ph) at least six hours of those readings to try to ensure that that is the reading. If it’s a little higher, we want to go for 24 hours. And if it’s up at 8,000 or 9,000, we would like to go 48 hours just to make sure it can sustain those pressures for that amount of time.  

Images from BP’s Oly Rov1 camera show the gauge for the input on the blowout preventer has been 2,000 psi for quite some time:

And the Hos ROV1 camera shows pressure of less than 1,000 bpi on another gauge:

However, as BP’s Kent Wells explained earlier today:

People still looking at pressure gauges and talking about that. The pressure sensing devices are what we call pressure transducers and they send a signal to the surface which are then are converted to their actual pressure readings. So we will not have ROV cameras on pressure gauges that will show what the pressures are during the tests. The pressure gauges you see are for our hydraulic equipment or (accumulators) et cetera like that.

So the gauges don’t necessarily mean anything.

The thing that worries me though is that BP closed down one or more valves, and substantially reduced the amount of oil gushing out. But perhaps 10 minutes after they started the test, they opened the valves all the way.

Now, the oil is gushing out full throttle:

The plan was to very gradually shut off more and more valves.

Given that BP opened the valves back open so quickly, I take that as a sign that the integrity test is failing. Hopefully I am wrong, and there will be good news tomorrow.

Hopefully, BP and the government are simply studying the data from the initial first couple of minutes of the test, recalibrating equipment or repairing the "choke line" leak which was discussed earlier today, and that the test will succeed.

But given BP’s track record, we may not find out until hours, days or even weeks after the results are in whether the test is a success or failure.

Subscribe
Notify of
0 Comments
Inline Feedbacks
View all comments

Stay Connected

156,328FansLike
396,312FollowersFollow
2,330SubscribersSubscribe

Latest Articles

0
Would love your thoughts, please comment.x
()
x